Have sinced had a GT3071 fitted and was hoping a larger a/r(old turbo was 0.64, current is 0.86) might solve the problem but it more or less felt the same.At the beginning of the week I had my downpipe back 2.5" mongoose replaced with a custom 3" one and what a difference!
I think its possible my problems were down to the step down from the 3" janspeed downpipe into a 2.5" mongoose decat as the car is now trying to make boost ridiculously fast, even on light throttle.In 3rd/4th even with less than half throttle the rate at which it zips from 0.5 to 1.2 bar(actuator pressure) is incredible.I haven't dared put my foot flat down as the car needs remapping to suit so god knows how fast it will spool with some welly.
Hoping to get it mapped shortly so will see for sure what's happened.Have asked Ed to dial in my 260 cams anyway.